When I was sent an older Disston backsaw to rehandle, it was requested that I reuse the saw bolts and medallion. While there was nothing wrong with them, they were too short to reach through the new and larger handle. While I could have sunk them below the surface of the handle, such a solution would have looked awkward and amateurish. Rejection of that option meant the reach of the bolt or nut had to be extended. I chose to extend the bolt.
To extend the bolt, I used a short length of 1/4″ brass rod. I began by drilling a 1/8″ hole in one end, to a depth of about 3/8″. I then trued that end up so that the face was perpendicular to the sides. Finally, I filed a couple of grooves into the face to give the solder an easy entry point into the joint.
Next, I chucked the medallion in the lathe, then took light cuts to remove the existing threads. Because I did not want to damage the head of the bolt, I did not tighten the chuck as much as I could have or normally would, so limited myself to light cuts. I took multiple passes until I had turned the bolt shank down to 1/8″.
With the bolt still in the lathe, I slipped the extension over the reduced shank on the bolt, then used a scrap of metal rod mounted in the tailstock to hold it in place while I joined them with silver-bearing solder.
With the extension in place, I turned to threading the new shank. Like Stanley, Disston used 12-20 threads, a size that has now fallen out of favor. 12-20 threads have a major diameter of 0.212 inches, so I first turned the extension down to that dimension in several light passes.
Because 12-20 threads are rarely used nowadays, the taps and dies needed to cut them are not commonly found items. While I do not own such a die, I do have a die head that can cut 12-20 threads in a pinch. Using 1/4″-20 chasers, I can adjust the die head to cut a 12-20 thread. I cut the threads in multiple light passes to prevent the cutting torque from spinning the bolt in the chuck. The video below shows a couple of those passes (the adjustment shown between threading passes reduces the diameter that the die cuts).
At the smallest setting, there was still a hint of a flat spot on the crest of the threads, so the nut would only thread on one or two turns before binding. With the lathe running, I used a three square needle file to finish off the thread.
And that’s it. After a little polishing on the lathe, these now look almost as good as new.
That’s going the extra mile. Bravo!
Thanks, Tico!
Isaac
Great job! It’s a wonder the head of the medaillion could be clamped in the chuck so well. I probably wouldn’t have trust it.
Kees,
I did wrap the head in paper to help protect it, but was still concerned that it might slip during threading. Got lucky, though, and was able to make it work by doing that in about ten or fifteen steps. Definitely not fast, but I couldn’t think of any better options.
Isaac